LT1 Based Engine Tech 1993-1997 LT1/LT4 Engine Related

Cam Install Help Needed?

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Old 03-21-2009, 11:12 PM
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Update:

I loaded the new tune on today. I started it up after turning it over some with the coil disconnected. I saw the oil pressure come up after a couple of short tries. I drove it around the neighborhood for a bit then found a spot to let it rip. (Staying under the speed limit of course) It had a miss and was running a little rough on acceleration so I had to turn around and get it back home. After playing with some of the wires I thought I saw a spark arching over to one of the headers. It was arching through the heat sock. I verified by grabbing the wire and shocking the crap out of myself. I tie wrapped it back and it should be good now. I also noticed an oil leak. It did not start until I took it for a drive and got on it a bit. It is leaking from the back of the intake where I put The Right Stuff across the China wall. The leak is right at the seam above the pipe that comes off the block. I tightened down the back 4 bolts again and ran a bunch more of The Rights Stuff along the seam with my finger. I don't know if that will help. I'm going for a long drive tomorrow about an hour away so we will see. Hopefully it will run smoother also. I thought I recorded a video to post then when I got on the computer I had a 2 second 60kb video. I guess I hit the button twice. I'll get another one tomorrow.

One thing I noticed is that seems a lot louder now. I think it is because the idle is set at 850 rpms. I'm wondering if this could be lowered some without effecting driveablity. If not it may be time for some bullet mufflers mufflers out back with cut outs up front.

Something new I noticed is that my belt tensioner pulley was bouncing up and down a little bit. Is this due to the lope of the new cam? I don't remember it doing that before.

Last edited by rickreeves1; 03-21-2009 at 11:17 PM.
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Old 03-22-2009, 06:28 PM
  #62  
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Update:

Well today didnt go all that well. I started out at 10:30am to head home from where I work on the car. It was leaking pretty bad from the rear of the intake. Lots of smoke was coming from under the hood and it was running a little rough. When I got home I deceided to pull the intake and reseal it again. I don't have many tools at home which made it a little more interesting. I had to run to Autozone twice and that same wire I had tied up yesterday to keep it from arching must have fell out so it ran really rough and backfired until I caught it. It took about two hours to pull the intake clean it and reseal. The front was actually sealed really well. Somehow the back didnt do so well. Right in the center where that bolt comes off the block it had very little sealer. After cleaning, I used the right stuff again along the back and front of the intake and up the china walls. This time I used a good bit more and did my best to cover it all and seat the intake only once. I didnt have my torque wrench so I had to feel for it. I followed the correct tightening pattern. I'm not going to start it until tomorrow morning which should give it about 15 hours to dry. Hopefilly all goes well.
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Old 03-23-2009, 12:11 PM
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Well I drove it to work this morning. The leak at the back of the intake appears to be gone. I didnt get on it hard so I'm not 100% sure yet but I didn't see any new oil leaking. It is running a little rough like there is a slight miss on acceleration. It also backfired once while accelerating normal. I will go back and check all 8 plugs again for fit. Any other ideas?

Here's a short datamaster file I was able to record this morning before the laptop died on me. I didnt get any good runs in. It's just a short cruise and some idleing. I need a new battery for the laptop. How's it look?

http://www.mediafire.com/file/zidwim...ll_3_23_09.uni


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Old 03-23-2009, 07:59 PM
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I think we found it!

I got home and checked everything over. I started with the spark plug wires and plugs. I pulled all the boots except for the most difficult 5 and 7. It got dark before I got to them. I hate those two. I also retightened the six plugs. Wire boot number 4 was a little loose. I pulled it off and the plug could easily be turned by hand either way. After I was done tightening I took it for a test drive around the neighborhood. No more bogging or backfiring. I only got up to about 30. I jumped in the car without my wallet and license. I guess I got a little too excited. If I remember correctly the same thing happened the last time I swapped spark plugs. One backed out after some driving. I change them at least once a year since they are cheap enough. I figure it's not a bad idea anyway with the N2O.

It also looks like the intake is holding well. No more visible leaks. If everything seems fine in the morning I'm going WOT for a little test.

I may go check for arching now. If my neighbor can mow the grass in the dark I can make a little engine noise.
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Old 03-24-2009, 11:00 AM
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Well the car died on my way to work today. All of the electronics started going out one by one untilit died. It was strange driving without the LCD. I was stuck on the side of the interstate for about 30 minutes until I found the alternator wiring harness was unplugged. Don't know who forgot to put that back on. GM hid that sucker pretty good under there. I think mine might have a clip missing which makes it easier to get off but probably also easier to vibrate off. Other than that it still seems to be running ok.

Here's a new Datamaster log file but it's probably all screwed up since it started to run rough and die near the end where I was loosing power. The DTC error codes for map low and EGR fault I believe are due to the low voltage.

http://www.mediafire.com/file/u5dtqy...ll_3_24_09.uni

If anyone wants to download Datamaster to read uni files it is at the link below. You also get 20 free recording sessions with the trial version but you would need the cables.

http://www.ttspowersystems.com/DataM...downloads.html

Last edited by rickreeves1; 03-24-2009 at 11:14 AM.
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Old 04-15-2009, 02:39 PM
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Everything has been running fine since. It feels even better than I expected. I was finally able to get a video. Anyone know how to embed a Youtube video on this forum?

http://www.youtube.com/watch?v=9EdR8DXz1mM


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Old 04-15-2009, 03:38 PM
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Sounds good Rick!! Any cam surge at part-throttle?
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